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Analysis of Instability and Control of Output Increase of an Industrial Chemical Reactor

 

作者: J. Thýn,   J. Výborný,  

 

期刊: Isotopenpraxis Isotopes in Environmental and Health Studies  (Taylor Available online 1990)
卷期: Volume 26, issue 5  

页码: 204-209

 

ISSN:0021-1915

 

年代: 1990

 

DOI:10.1080/10256019008624279

 

出版商: Taylor & Francis Group

 

关键词: industrial plants;mathematical models;response function;simulation;tracer techniques

 

数据来源: Taylor

 

摘要:

Intensification of production of aldehydes by an exothermic catalysed reaction of propylen and synthese gas (so called hydroformylation) due to higher flow rates of propylene led to unstable operation of reactor. The problem of stabilisation had to be solved, i.e. the reasons for instabilities had to be found and then the method of control of transition to the higher stabilised production had to be proposed. Information obtained by the experimental methods of stimulus-response directly on the industrial unit (record of responses of concentrations of the radiotracer and of the temperatures of the cooling media in the reactor) were used in mathematical modelling of the reactor dynamics. The knowledge accumulated by simulation of the process by proposed physico-chemical model enabled control of operation of the reactor at transition to the higher requires output.

 

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