Analysis of Instability and Control of Output Increase of an Industrial Chemical Reactor
作者:
J. Thýn,
J. Výborný,
期刊:
Isotopenpraxis Isotopes in Environmental and Health Studies
(Taylor Available online 1990)
卷期:
Volume 26,
issue 5
页码: 204-209
ISSN:0021-1915
年代: 1990
DOI:10.1080/10256019008624279
出版商: Taylor & Francis Group
关键词: industrial plants;mathematical models;response function;simulation;tracer techniques
数据来源: Taylor
摘要:
Intensification of production of aldehydes by an exothermic catalysed reaction of propylen and synthese gas (so called hydroformylation) due to higher flow rates of propylene led to unstable operation of reactor. The problem of stabilisation had to be solved, i.e. the reasons for instabilities had to be found and then the method of control of transition to the higher stabilised production had to be proposed. Information obtained by the experimental methods of stimulus-response directly on the industrial unit (record of responses of concentrations of the radiotracer and of the temperatures of the cooling media in the reactor) were used in mathematical modelling of the reactor dynamics. The knowledge accumulated by simulation of the process by proposed physico-chemical model enabled control of operation of the reactor at transition to the higher requires output.
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